This patch fixes the PTP Tx timestamp interrupt handler. The original
code misinterpreted the interrupt handler design. We were clearing the
ena_mask bit for the Timesync interrupts. This is done to indicate that
the interrupt will be handled in a scheduled work item (instead of
immediately) and that work item is responsible for re-enabling the
interrupts. However, the Tx timestamp was being handled immediately and
nothing was ever re-enabling it. This resulted in a single interrupt
working for the life of the driver.
This patch fixes the issue by instead clearing the bit from icr0 which
is used to indicate that the interrupt was immediately handled and can
be re-enabled right away. This patch also clears up a related issue due
to writing the PRTTSYN_STAT_0 register, which was unintentionally
clearing the cause bits for Timesync interrupts.
Change-ID: I057bd70d53c302f60fab78246989cbdfa469d83b
Signed-off-by: Jacob Keller <jacob.e.keller@intel.com>
Acked-by: Anjali Singhai Jain <anjali.singhai@intel.com>
Acked-by: Shannon Nelson <shannon.nelson@intel.com>
Tested-by: Kavindya Deegala <kavindya.s.deegala@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Merge tag 'linux-can-fixes-for-3.15-20140424' of git://gitorious.org/linux-can/linux-can
Marc Kleine-Budde says:
====================
this is a pull request for net/master, for the v3.15 release cycle, consisting
of 26 patches.
Thomas Gleixner contributes 21 patches for the c_can driver, which address
several shortcomings in the driver like hardware initialisation, concurrency,
message ordering and poor performance. Two patches Oliver Hartkopp, one adds a
missing lock to the sja1000_isa driver, the other one fixes the return value in
the generic bit time configuration function. And finally a patch by Alexander
Stein, that fixes the slcan driver to use the correct spinlock variant.
To make it 26 patches, Wolfgang Grandegger patch for the c_can_pci
driver, which enables the bus master only for MSI and a patch by
Wolfram Sang, which converts the 'instance' in the c_can driver to the
proper type.
====================
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch changes the name used by Ethtool to something more
conventional in preparation for TSE Ethtool register dump
support to be added in the near future.
Signed-off-by: Vince Bridgers <vbridgers2013@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch addresses a fault in the error recovery path of the probe
routine where the netdev structure was not being unregistered properly
leading to a panic only when the phy probe failed.
Abbreviated panic stack seen is as follows:
(free_netdev+0xXX) from (altera_tse_probe+0xXX)
(altera_tse_probe+0xXX) from (platform_drv_probe+0xXX)
(platform_drv_probe+0xXX) from (driver_probe_device+0xXX)
(driver_probe_device+0xXX) from (__driver_attach+0xXX)
(__driver_attach+0xXX) from (bus_for_each_dev+0xXX)
(bus_for_each_dev+0xXX) from (driver_attach+0xXX)
(driver_attach+0xXX) from (bus_add_driver+0xXX)
(bus_add_driver+0xXX) from (driver_register+0xXX)
(driver_register+0xXX) from (__platform_driver_register+0xXX)
(__platform_driver_register+0xXX) from (altera_tse_driver_init+0xXX)
(altera_tse_driver_init+0xXX) from (do_one_initcall+0xXX)
(do_one_initcall+0xXX) from (kernel_init_freeable+0xXX)
(kernel_init_freeable+0xXX) from (kernel_init+0xXX)
(kernel_init+0xXX) from (ret_from_fork+0xXX)
Signed-off-by: Vince Bridgers <vbridgers2013@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch initializes the pause quanta set for transmitted pause frames
to the IEEE specified default of 0xffff.
Signed-off-by: Vince Bridgers <vbridgers2013@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch works around a recently discovered unaligned receive dma problem
with the Altera SGMDA. The Altera SGDMA component cannot be configured to
DMA data to unaligned addresses for receive packet operations from the
Triple Speed Ethernet component because of a potential data transfer
corruption that can occur. This patch addresses this issue by
utilizing the shift 16 bits feature of the Altera Triple Speed Ethernet
component and modifying the receive buffer physical addresses accordingly
such that the target receive DMA address is always aligned on a 32-bit
boundary.
Signed-off-by: Vince Bridgers <vbridgers2013@gmail.com>
Tested-by: Matthew Gerlach <mgerlach@altera.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Starting with commit 2dc33bbc "bnx2x: Remove the sriov VFOP mechanism",
the bnx2x started enforcing vlan credits for all vlan configurations.
This exposed 2 issues:
- Vlan credits are not returned once a VF is removed; this causes a leak
of credits, and eventually will lead to VFs with no vlan credits.
- A vlan credit must be set aside for the Hypervisor to use, and should
not be visible to the VF.
Although linux VFs at the moment do not support vlan configuration [from the
VF side] which causes them to be resilient to this sort of issue, Windows VF
over linux hypervisors might fail to load as the vlan credits become depleted.
Signed-off-by: Yuval Mintz <Yuval.Mintz@qlogic.com>
Signed-off-by: Ariel Elior <Ariel.Elior@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
When removing a VF interface, the driver fails to release that VF's mailbox
and bulletin board allocated memory.
Signed-off-by: Yuval Mintz <Yuval.Mintz@qlogic.com>
Signed-off-by: Ariel Elior <Ariel.Elior@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
slc_xmit is called within softirq context and locks sl->lock, but
slcan_write_wakeup is not softirq context, so we need to use
spin_[un]lock_bh!
Detected using kernel lock debugging mechanism.
Signed-off-by: Alexander Stein <alexander.stein@systec-electronic.com>
Acked-by: Oliver Hartkopp <socketcan@hartkopp.net>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
When trying to set a data bitrate on non CAN FD devices the 'ip' tool
answers with:
RTNETLINK answers: Unknown error 524
Rename '-ENOTSUPP' to '-EOPNOTSUPP' so that 'ip' answers correctly:
RTNETLINK answers: Operation not supported
Signed-off-by: Oliver Hartkopp <socketcan@hartkopp.net>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
When accessing the SJA1000 controller registers in the indirect access mode,
writing the register number and reading/writing the data has to be an atomic
attempt.
As the sja1000_isa driver is an old style driver with a fixed number of
instances the locking variable depends on the same index like all the other
configuration elements given on the module command line.
As a positive side effect dev->dev_id is populated by the instance index,
which was missing in 3e66d0138c ("can: populate netdev::dev_id for udev
discrimination").
Reported-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Oliver Hartkopp <socketcan@hartkopp.net>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Coverity complains that c_can_pci_probe() calls pci_enable_msi() without
checking the result:
CID 712278 (#1 of 1): Unchecked return value (CHECKED_RETURN) 3. check_return:
Calling pci_enable_msi_block without checking return value (as is done
elsewhere 88 out of 105 times).
88 pci_enable_msi(pdev);
This is CID 712278.
Signed-off-by: Wolfgang Grandegger <wg@grandegger.com>
Reported-by: Bjorn Helgaas <bhelgaas@google.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Commit 6439fbce10 (can: c_can: fix error checking of priv->instance in
probe()) found the warning but applied a suboptimal solution. Since, both
pdev->id and of_alias_get_id() return integers, it makes sense to convert the
variable to an integer and avoid the cast.
Signed-off-by: Wolfram Sang <wsa@sang-engineering.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
It's suffcient to kill the TXIE bit in the message control register
even if the documentation of C and D CAN says that it's not allowed to
do that while MSGVAL is set. Reality tells a different story and this
change gives us another 2% of CPU back for not waiting on I/O.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Mark suggested to use one IF for the softirq and the other for the
xmit function to avoid the xmit lock.
That requires to write the frame into the interface first, then handle
the echo skb and store the dlc before committing the TX request to the
message ram.
We use an atomic to handle the active buffers instead of reading the
MSGVAL register as thats way faster especially on PCH/x86.
Suggested-by: Mark <mark5@del-llc.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Instead of obfuscating the code by artificial 16 bit splits use the
proper 32 bit assignments and split the result when writing to the
interface.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Remove the MASK from the TX transfer side.
Make the code readable and get rid of the annoying IFX_WRITE_XXX_16BIT
macros which are just obfuscating the code.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Sigh!
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Alexander reported that the new optimized handling of the RX fifo
causes random packet loss on Intel PCH C_CAN hardware.
After a few fruitless debugging sessions I got hold of a PCH (eg20t)
afflicted system. That machine does not have the CAN interface wired
up, but it was possible to reproduce the issue with the HW loopback
mode.
As Alexander observed correctly, clearing the NewDat flag along with
reading out the message buffer causes that issue on C_CAN, while D_CAN
handles that correctly.
Instead of restoring the original message buffer handling horror the
following workaround solves the issue:
transfer buffer to IF without clearing the NewDat
handle the message
clear NewDat bit
That's similar to the original code but conditional for C_CAN.
I really wonder why all user manuals (C_CAN, Intel PCH and some more)
recommend to clear the NewDat bit right away. The knows it all Oracle
operated by Gurgle does not unearth any useful information either. I
simply cannot believe that we are the first to uncover that HW issue.
Reported-and-tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
The RX buffer split causes packet loss in the hardware:
What happens is:
RX Packet 1 --> message buffer 1 (newdat bit is not cleared)
RX Packet 2 --> message buffer 2 (newdat bit is not cleared)
RX Packet 3 --> message buffer 3 (newdat bit is not cleared)
RX Packet 4 --> message buffer 4 (newdat bit is not cleared)
RX Packet 5 --> message buffer 5 (newdat bit is not cleared)
RX Packet 6 --> message buffer 6 (newdat bit is not cleared)
RX Packet 7 --> message buffer 7 (newdat bit is not cleared)
RX Packet 8 --> message buffer 8 (newdat bit is not cleared)
Clear newdat bit in message buffer 1
Clear newdat bit in message buffer 2
Clear newdat bit in message buffer 3
Clear newdat bit in message buffer 4
Clear newdat bit in message buffer 5
Clear newdat bit in message buffer 6
Clear newdat bit in message buffer 7
Clear newdat bit in message buffer 8
Now if during that clearing of newdat bits, a new message comes in,
the HW gets confused and drops it.
It does not matter how many of them you clear. I put a delay between
clear of buffer 1 and buffer 2 which was long enough that the message
should have been queued either in buffer 1 or buffer 9. But it did not
show up anywhere. The next message ended up in buffer 1. So the
hardware lost a packet of course without telling it via one of the
error handlers.
That does not happen on all clear newdat bit events. I see one of 10k
packets dropped in the scenario which allows us to reproduce. But the
trace looks always the same.
Not splitting the RX Buffer avoids the packet loss but can cause
reordering. It's hard to trigger, but it CAN happen.
With that mode we use the HW as it was probably designed for. We read
from the buffer 1 upwards and clear the buffer as we get the
message. That's how all microcontrollers use it. So I assume that the
way we handle the buffers was never really tested. According to the
public documentation it should just work :)
Let the user decide which evil is the lesser one.
[ Oliver Hartkopp: Provided a sane config option and help text and
made me switch to favour potential and unlikely reordering over
packet loss ]
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
The driver handles pointlessly TWO interrupts per packet. The reason
is that it enables the status interrupt which fires for each rx and tx
packet and it enables the per message object interrupts as well.
The status interrupt merily acks or in case of D_CAN ignores the TX/RX
state and then the message object interrupt fires.
The message objects interrupts are only useful if all message objects
have hardware filters activated.
But we don't have that and its not simple to implement in that driver
without rewriting it completely.
So we can ditch the message object interrupts and handle the RX/TX
right away from the status interrupt. Instead of TWO we handle ONE.
Note: We must keep the TXIE/RXIE bits in the message buffers because
the status interrupt alone is not reliable enough in corner cases.
If we ever have the need for HW filtering, then this code needs a
complete overhaul and we can think about it then. For now we prefer a
lower interrupt load.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
On D_CAN the RXOK, TXOK and LEC bits are cleared/set on read of the
status register. No need to update them.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Instead of writing to the message object we can simply clear the
NewDat bit with the get method.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
If the allocation of the error skb fails, we still want to see the
error statistics.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Reading the LEC type with
return (mode & ENABLED) && (status & LEC_MASK);
is not guaranteed to return (status & LEC_MASK) if the enabled bit in
mode is set. It's guaranteed to return 0 or !=0.
Remove the inline function and call unconditionally into the
berr_handling code and return early when the reporting is disabled.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
If the allocation of an error skb fails, the state change handling
returns w/o doing any work. That leaves the interface in a wreckaged
state as the internal status is wrong.
Split the interface handling and the skb handling.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
There is no guarantee that the skb is in the same state after calling
net_receive_skb(). It might be freed or reused. Not really harmful as
its a read access, except you turn on the proper debugging options
which catch a use after free.
The whole can subsystem is full of this. Copy and paste ....
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
The state change handler is called with device interrupts disabled
already. So no point in disabling them again when we enter bus off
state.
But what's worse is that we reenable the interrupts at the end of NAPI
poll unconditionally. So c_can_start() which is called from the
restart timer can trigger interrupts which confuse the hell out of the
half reinitialized driver/hw.
Remove the pointless device interrupt disable in the BUS_OFF handler
and prevent reenabling the device interrupts at the end of the poll
routine when the current state is BUS_OFF.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
c_can_start() enables interrupts way too early. The first enabling
happens when setting the control mode in c_can_chip_config() and then
again at the end of the function.
But that happens before napi_enable() and that means that an interrupt
which comes in will disable interrupts again and call napi_schedule,
which ignores the request and the later napi_enable() is not making
thinks work either. So the interface is up with all device interrupts
disabled.
Move the device interrupt after napi_enable() and add it to the other
callsites of c_can_start() in c_can_set_mode() and c_can_power_up()
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
All type checks in c_can.c are != BOSCH_D_CAN so nobody noticed so far
that the pci code does not update the type information.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
This fixes a seg fault on 'ethtool -A' entry if the
interface is down. Obviously we need to have the
phy device initialized / "connected" (see of_phy_connect())
to be able to advertise pause frame capabilities.
Fixes: 23402bddf9
Signed-off-by: Claudiu Manoil <claudiu.manoil@freescale.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
o In case QLC_83XX_MBX_CMD_NO_WAIT command type the calling
function does not free the memory as it does not wait for
response. So free it when get a response from adapter after
sending the command.
Signed-off-by: Rajesh Borundia <rajesh.borundia@qlogic.com>
Signed-off-by: Shahed Shaikh <shahed.shaikh@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Some firmware versions fails to reset the lock during
initialization. Force reset firmware API lock during driver
probe to ensure lock availability.
Signed-off-by: Sony Chacko <sony.chacko@qlogic.com>
Signed-off-by: Shahed Shaikh <shahed.shaikh@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
There are two breaks missing there. The result is that userspace
receives multiple messages which might be confusing.
Introduced-by: 3d249d4c "net: introduce ethernet teaming device"
Signed-off-by: Jiri Pirko <jiri@resnulli.us>
Signed-off-by: David S. Miller <davem@davemloft.net>
I was told that the Cadence macb driver is also useful on Microblaze.
Signed-off-by: Jean Delvare <jdelvare@suse.de>
Cc: Nicolas Ferre <nicolas.ferre@atmel.com>
Cc: David S. Miller <davem@davemloft.net>
Cc: Michal Simek <monstr@monstr.eu>
Cc: Mark Brown <broonie@kernel.org>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Redefine some macros that were conditioned upon SMC_DEBUG level.
By allowing compiler to verify parameters used by these macros
unconditionally, we can flag compilation failures.
Compiler will still optimize out the unused code path depending on
SMC_DEBUG, so this is a net gain.
Signed-off-by: Joe Perches <joe@perches.com>
Signed-off-by: Zi Shen Lim <zlim.lnx@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The goal of this patch is to fix rtnelink notification. The main problem was
about notification for fdb entry with more than one remote. Before the patch,
when a remote was added to an existing fdb entry, the kernel advertised the
first remote instead of the added one. Also when a remote was removed from a fdb
entry with several remotes, the deleted remote was not advertised.
Signed-off-by: Nicolas Dichtel <nicolas.dichtel@6wind.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
In ksz9021_load_values_from_of() val2 to val4 aren't tested against their
initialization value.
This causes the test to always succeed, and this value to be used as if it
was loaded from the devicetree instead of being ignored, in case of a
missing/invalid property in the ethernet OF device node.
As a result, the value "0" is written to the relevant registers.
Change the conditions to test against the right initialization value.
Signed-off-by: Hubert Chaumette <hchaumette@adeneo-embedded.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
When SMC_DEBUG >= 2, we hit the following compilation error:
drivers/net/ethernet/smsc/smc91x.c:85:0:
drivers/net/ethernet/smsc/smc91x.c: In function ‘smc_findirq’:
drivers/net/ethernet/smsc/smc91x.c:1784:9: error: ‘dev’ undeclared (first use in this function)
DBG(2, dev, "%s: %s\n", CARDNAME, __func__);
^
Fix it by passing in the appropriate netdev pointer.
Signed-off-by: Zi Shen Lim <zlim.lnx@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch adds phy_found error path when there is no phy device
and changes bus_name.
Signed-off-by: Byungho An <bh74.an@samsung.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch moves cksum_ctl to tx_rd_des23 from cksum_pktlen for correct checksum
offloading and modifies size for Tx/Rx descriptor.
Signed-off-by: Byungho An <bh74.an@samsung.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Execute "ethtool -L eth0 combined 0" in guest, if multiqueue
is enabled, virtnet_send_command() will return -EINVAL error,
there is a validation in QEMU.
But if multiqueue is disabled, virtnet_set_queues() will just
return zero (success). We should return error for this situation.
Signed-off-by: Amos Kong <akong@redhat.com>
Acked-by: Jason Wang <jasowang@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The MAC address retrieved from dt was not actually written to the
hardware. This meant proper communication was only possible after
changing the MAC address.
Fix that by always writing the mac address during probing.
Signed-off-by: Max Schwarz <max.schwarz@online.de>
Acked-by: Heiko Stuebner <heiko@sntech.de>
Tested-by: Heiko Stuebner <heiko@sntech.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
Add \n at the end of messages where missing, remove all \r.
Reported-by: Joe Perches <joe@perches.com>
Signed-off-by: Jakub Kicinski <kubakici@wp.pl>
Tested-by: Aaron Brown <aaron.f.brown@intel.com>
Tested-by: Phil Schmitt <phillip.j.schmitt@intel.com>
Tested-by: Kavindya Deegala <kavindya.s.deegala@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>