Rather than hardcode 9600, use the existing default_baud parameter (which
also defaults to 9600).
Signed-off-by: Darren Hart <dvhart@linux.intel.com>
CC: Tomoya MORINAGA <tomoya.rohm@gmail.com>
CC: Feng Tang <feng.tang@intel.com>
CC: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
For cases where boards with non-default clocks are not yet added to the kernel
or when the clock varies across hardware revisions, it is useful to be
able to specify the UART clock on the kernel command line.
Add the user_uartclk parameter and prefer it, if set, to the default and
board specific UART clock settings. Specify user_uartclock on the command-line
with "pch_uart.user_uartclk=48000000".
Signed-off-by: Darren Hart <dvhart@linux.intel.com>
CC: Tomoya MORINAGA <tomoya.rohm@gmail.com>
CC: Feng Tang <feng.tang@intel.com>
CC: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add support for the Fish River Island II (FRI2) UART clock following the CM-iTC
quirk handling mechanism. Depending on the firmware installed on the device, the
FRI2 uses a 48MHz or a 64MHz UART clock. This is detected with DMI strings.
Add similar UART clock quirk handling to the pch_console_setup() function to
enable kernel messages on boards with non-standard UART clocks.
Per Alan's suggestion, abstract out UART clock selection into
pch_uart_get_uartclk() to avoid code duplication.
Signed-off-by: Darren Hart <dvhart@linux.intel.com>
CC: Tomoya MORINAGA <tomoya.rohm@gmail.com>
CC: Feng Tang <feng.tang@intel.com>
CC: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The term "base baud" refers to the fastest baud rate the device can communicate
at. This is clock/16. pch_uart is using base_baud as the clock itself. Rename
the variables to be semantically correct.
Signed-off-by: Darren Hart <dvhart@linux.intel.com>
CC: Tomoya MORINAGA <tomoya.rohm@gmail.com>
CC: Feng Tang <feng.tang@intel.com>
CC: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The runtime PM of sh-sci devices is enabled when sci_probe() returns,
so the pm_runtime_put_sync() executed by driver_probe_device()
attempts to suspend the device. Then, in some situations, a
diagnostic message is printed to the console by one of the runtime
suspend routines handling the sh-sci device, which causes synchronous
runtime resume to be started from the device's own runtime suspend
callback. This causes rpm_resume() to be run eventually, which sees
the RPM_SUSPENDING status set by rpm_suspend() and waits for it to
change. However, the device's runtime PM status cannot change at
that point, because the routine that has set it waits for the
rpm_suspend() to return. A deadlock occurs as a result.
To avoid that make sci_init_single() increment the device's
runtime PM usage counter, so that it cannot be suspended by
driver_probe_device(). That counter has to be decremented
eventually, so make sci_startup() do that before starting to
actually use the device and make sci_shutdown() increment it
again before returning to balance the incrementation carried out by
sci_startup().
Signed-off-by: Rafael J. Wysocki <rjw@sisk.pl>
Tested-by: Kuninori Morimoto <kuninori.morimoto.gx@renesas.com>
Signed-off-by: Paul Mundt <lethal@linux-sh.org>
The PowerPC legacy iSeries platform is being removed so this is no
longer selectable.
Cc: Alan Cox <alan@linux.intel.com>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Cc: linux-serial@vger.kernel.org
Signed-off-by: Stephen Rothwell <sfr@canb.auug.org.au>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
The PowerPC legacy iSeries platform is being removed, so this code is no
longer needed.
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Stephen Rothwell <sfr@canb.auug.org.au>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
In addition to the /32 prescaler, the MPC5200B supports a second
baudrate prescaler /4 to reach higher baudrates.
The current calculation (introduced with commit 0d1f22e4) in the kernel
preferes this low prescaler as often as possible, but with some
imprecise counterparts the communication on low baudrates fails.
According a support-mail from freescale the low prescaler (/4) allows
just 1% tolerance in bittiming in contrast to 4% of the high prescaler
(/32). The prescaler not only affects the baudrate-calculation, but
also the sampling of the bits on the wire.
With this patch, we use the slightly less precise, but higher tolerant
prescaler calculation on low baudrates up to (and including) 115200 baud
and the more precise calculation above.
Tested on a custom MPC5200B board with "fsl,mpc5200b-psc-uart".
Calculation Examples with prescaler (PS) 4 and 32 and divisor (DIV) on
various baudrates. Real stands for the real baudrate generated and Diff
for the differences between:
50 Baud PS 32 DIV 0xa122 Real 50 Diff 0.00%
75 Baud PS 32 DIV 0x6b6c Real 75 Diff 0.00%
110 Baud PS 32 DIV 0x493e Real 110 Diff 0.00%
134 Baud PS 32 DIV 0x3c20 Real 133 Diff 0.75%
150 Baud PS 32 DIV 0x35b6 Real 150 Diff 0.00%
200 Baud PS 32 DIV 0x2849 Real 199 Diff 0.50%
300 Baud PS 4 DIV 0xd6d8 Real 300 Diff 0.00%
PS 32 DIV 0x1adb Real 300 Diff 0.00%
600 Baud PS 4 DIV 0x6b6c Real 600 Diff 0.00%
PS 32 DIV 0x0d6e Real 599 Diff 0.17%
1200 Baud PS 4 DIV 0x35b6 Real 1200 Diff 0.00%
PS 32 DIV 0x06b7 Real 1199 Diff 0.08%
1800 Baud PS 4 DIV 0x23cf Real 1799 Diff 0.06%
PS 32 DIV 0x047a Real 1799 Diff 0.06%
2400 Baud PS 4 DIV 0x1adb Real 2400 Diff 0.00%
PS 32 DIV 0x035b Real 2401 Diff - 0.04%
4800 Baud PS 4 DIV 0x0d6e Real 4799 Diff 0.02%
PS 32 DIV 0x01ae Real 4796 Diff 0.08%
9600 Baud PS 4 DIV 0x06b7 Real 9598 Diff 0.02%
PS 32 DIV 0x00d7 Real 9593 Diff 0.07%
19200 Baud PS 4 DIV 0x035b Real 19208 Diff - 0.04%
PS 32 DIV 0x006b Real 19275 Diff - 0.39%
38400 Baud PS 4 DIV 0x01ae Real 38372 Diff 0.07%
PS 32 DIV 0x0036 Real 38194 Diff 0.54%
57600 Baud PS 4 DIV 0x011e Real 57692 Diff - 0.16%
PS 32 DIV 0x0024 Real 57291 Diff 0.54%
76800 Baud PS 4 DIV 0x00d7 Real 76744 Diff 0.07%
PS 32 DIV 0x001b Real 76388 Diff 0.54%
115200 Baud PS 4 DIV 0x008f Real 115384 Diff - 0.16%
PS 32 DIV 0x0012 Real 114583 Diff 0.54%
153600 Baud PS 4 DIV 0x006b Real 154205 Diff - 0.39%
PS 32 DIV 0x000d Real 158653 Diff - 3.29%
230400 Baud PS 4 DIV 0x0048 Real 229166 Diff 0.54%
PS 32 DIV 0x0009 Real 229166 Diff 0.54%
307200 Baud PS 4 DIV 0x0036 Real 305555 Diff 0.54%
PS 32 DIV 0x0007 Real 294642 Diff 4.09%
460800 Baud PS 4 DIV 0x0024 Real 458333 Diff 0.54%
PS 32 DIV 0x0005 Real 412500 Diff 10.48%
500000 Baud PS 4 DIV 0x0021 Real 500000 Diff 0.00%
PS 32 DIV 0x0004 Real 515625 Diff - 3.13%
576000 Baud PS 4 DIV 0x001d Real 568965 Diff 1.22%
PS 32 DIV 0x0004 Real 515625 Diff 10.48%
614400 Baud PS 4 DIV 0x001b Real 611111 Diff 0.54%
PS 32 DIV 0x0003 Real 687500 Diff -11.90%
921600 Baud PS 4 DIV 0x0012 Real 916666 Diff 0.54%
PS 32 DIV 0x0002 Real 1031250 Diff -11.90%
1000000 Baud PS 4 DIV 0x0011 Real 970588 Diff 2.94%
PS 32 DIV 0x0002 Real 1031250 Diff - 3.13%
1152000 Baud PS 4 DIV 0x000e Real 1178571 Diff - 2.31%
PS 32 DIV 0x0002 Real 1031250 Diff 10.48%
1500000 Baud PS 4 DIV 0x000b Real 1500000 Diff 0.00%
PS 32 DIV 0x0001 Real 2062500 Diff -37.50%
2000000 Baud PS 4 DIV 0x0008 Real 2062500 Diff - 3.13%
PS 32 DIV 0x0001 Real 2062500 Diff - 3.13%
2500000 Baud PS 4 DIV 0x0007 Real 2357142 Diff 5.71%
PS 32 DIV 0x0001 Real 2062500 Diff 17.50%
3000000 Baud PS 4 DIV 0x0006 Real 2750000 Diff 8.33%
PS 32 DIV 0x0001 Real 2062500 Diff 31.25%
3500000 Baud PS 4 DIV 0x0005 Real 3300000 Diff 5.71%
PS 32 DIV 0x0001 Real 2062500 Diff 41.07%
4000000 Baud PS 4 DIV 0x0004 Real 4125000 Diff - 3.13%
PS 32 DIV 0x0001 Real 2062500 Diff 48.44%
Signed-off-by: Frank Benkert <frank.benkert@avat.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is supposed to be doing a shift before the comparison instead of
just doing a bitwise AND directly. The current code means the start()
just returns without doing anything.
Signed-off-by: Dan Carpenter <dan.carpenter@oracle.com>
Acked-by: Jiri Slaby <jslaby@suse.cz>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Again, no need to duplicate the code. Let's use the helper.
Amiserial changes are only free of compilation errors. I have no
access to the hardware.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Hmm, the code was sleeping with interrupts disabled. This was not
good. Fix this by turning interrupts at an appropriate place. (The
race is protected by CLOSING flag.)
After the move, the code is identical to tty_port_close_end, so use
it!
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a preparation for a switch to tty_port_block_til_ready. We
need amiga_carrier_raised and amiga_dtr_rts. The implementation is
taken from startup, shutdown and current block_til_ready.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
amiserial is the last user of serialP.h. Let's move struct
serial_state directly to amiserial and remove serialP crap from
includes. Finally, remove the header from the tree completely.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
* instead of line, use tty->index or iterator...
* irq and type are left unset. So get rid of them.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
And use it to make the code more readable.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This changes flags' type to ulong which is appropriate for all the
set/clear_bits performed in the drivers..
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Nothing special. Just remove count from serial_state and change all
users to use tty_port.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Note that previously simserial set the delay to 0. So we preserve
that. BUT, is it correct?
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add tty_port to serial_state and start using common tty port members
from tty_port in amiserial and simserial. The rest will follow one by
one.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This avoids pain with tty refcounting and touching tty_port in the
future. It allows us to remove some info->tty tests because the tty
passed down to them can never be NULL.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Do not copy whole serial_state. We only need to know whether the speed
is to be changed. Hence store the info in advance and use it later.
A simple bool is enough.
Also remove reduntant assignments and move the tests directly to the
'if'.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is the final step to get rid of the one of the structures. A
further cleanup will follow. And I struct serial_state deserves cease
to exist after a switch to tty_port too.
While changing the lines, it removes also pointless tty->driver_data
casts.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
They used to work as a storage for 'info' pointer used in ISRs. They
are not really needed. Just pass the pointer through request_irq to
the handlers.
It was set to NULL and tested in the ISRs, but we do not need the
tests as we disable all the interrupts at the same places where NULL
sets were.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This means:
* close_delay
* closing_wait
* line
* port
* xmit_fifo_size
This actually fixes a bug in amiserial. It initializes one and uses
the other of the close delays. Yes, duplicating structure members is
evil.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Huh, why would one want to store two copies of them? Get rid of the
one from async_struct. That structure is going away as a whole soon.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
tty_wakeup is safe to be called from all contexts. No need to schedule
a tasklet for that. Let's call it directly like in other drivers.
This allows us to kill another member of async_struct structure. (If
we remove the dummy uses in simserial.)
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
First, remove unused macro and rs_multiport_struct structure. Nobody
uses them at all.
Further, the 2 drivers (they are below) which use the rest of
structures from serialP.h (async_struct and serial_state) do not use
all the members. Remove the members:
* which are unused or
* which are only initialized and never used for something real.
Everybody should avoid the structures with a looong distance.
Finally, remove the ALPHA kludge MCR quirks. They are 1:1 copy from
8250.h. No need to redefine them here.
The 2 promised users of the structures:
arch/ia64/hp/sim/simserial.c
drivers/tty/amiserial.c
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Geert Uytterhoeven <geert@linux-m68k.org>
Cc: Tony Luck <tony.luck@intel.com>
Cc: Fenghua Yu <fenghua.yu@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
All of them do not use the ugly interface defined in that header.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
It uses pointers to pci_dev, but compiler complains it doesn't know
it:
In file included from .../m32r_sio.c:53:
.../m32r_sio.h:21: warning: "struct pci_dev" declared inside parameter list
.../m32r_sio.h:21: warning: its scope is only this definition or declaration, which is probably not what you want
.../m32r_sio.h:22: warning: "struct pci_dev" declared inside parameter list
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
We want to know the value of the atomic variable in intr_connect after
the increment. But atomic_inc doesn't, per definition, return the
value. It is just a pure coincidence that ia64 defines atomic_inc as
atomic_inc_return.
So fix this mistake by using atomic_inc_return properly.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
* do not test if tty->index is in bounds. It is always.
* tty->index is not a minor! Fix that.
>From now on, let's assume that the parameter of the function is tty
index with base being zero. This makes also the code more readable.
Factually, there is no real change as tty_driver->minor_start is zero,
so the tests are equivalent. But it did not make sense. And if this
had changed eventually, it would have caused troubles.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Acked-by: Jiri Kosina <jkosina@suse.cz>
Cc: David Sterba <dsterba@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Checking if tty->index is in bounds is not needed. The tty has the
index set in the initial open. This is done in get_tty_driver. And it
can be only in interval <0,driver->num).
So remove the tests which check exactly this interval. Some are
left untouched as they check against the current backing device count.
(Leaving apart that the check is racy in most of the cases.)
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is from tty_reopen:
struct tty_driver *driver = tty->driver;
...
tty->driver = driver;
and it doesn't make sense at all. The driver is intended to be set in
initialize_tty_struct from tty_init_dev (initial open). So this set in
tty_reopen is not needed.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Remove the useless local variable and return the value itself.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
All num, magic and owner are set by alloc_tty_driver. No need to
re-set them on each allocation site.
pti driver sets something different to what it passes to
alloc_tty_driver. It is not a bug, since we don't use the lines
parameter in any way. Anyway this is fixed, and now we do the right
thing.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Acked-by: Tilman Schmidt <tilman@imap.cc>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Like the rest of the kernel, make a stub from alloc_tty_driver which
calls __alloc_tty_driver with proper owner. This will save us one more
assignment on the driver side.
Also this fixes some drivers which didn't set the owner. This allowed
user to remove the module from the system even though a tty from the
driver is still open.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
TTY buffer head and tail are initialized in tty_buffer_init. No need
to do it once again in initialize_tty_struct where tty_buffer_init is
called.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
We leave the existing paste mess alone and just fix up the vt side of
things.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Some of this ventures into selection which is still a complete lost cause. We
are not making it any worse. It's completely busted anyway.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
At this point we have the tty_lock guarding a couple of oddities, plus the
translation and unimap still.
We also extend the console_lock in a couple of spots where coverage is wrong
and switch vcs_open to use the right lock !
[Fixed the locking issue Jiri reported]
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The font methods are console_lock covered. Unfortunately they don't extend
the lock over all the needed tests.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
TIOCSERGETLSR should be saved in a uint so the cast here to unsigned
long is a bug.
Reported-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Dan Carpenter <dan.carpenter@oracle.com>
Acked-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The following commit: be4b028195
(tty: serial: OMAP: block idle while the UART is transferring data in PIO mode),
is introducing an oops if OMAP is booted using device tree blob because
the pdata will not be initialized.
Check if pdata is set before de-referencing it.
Signed-off-by: Benoit Cousson <b-cousson@ti.com>
Reviewed-by: Paul Walmsley <paul@pwsan.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Keyboard struct lifetime is easy, but the locking is not and is completely
ignored by the existing code. Tackle this one head on
- Make the kbd_table private so we can run down all direct users
- Hoick the relevant ioctl handlers into the keyboard layer
- Lock them with the keyboard lock so they don't change mid keypress
- Add helpers for things like console stop/start so we isolate the poking
around properly
- Tweak the braille console so it still builds
There are a couple of FIXME locking cases left for ioctls that are so hideous
they should be addressed in a later patch. After this patch the kbd_table is
private and all the keyboard jiggery pokery is in one place.
This update fixes speakup and also a memory leak in the original.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
* 'dt' of git://github.com/hzhuang1/linux: (6 commits)
Document: devicetree: add OF documents for arch-mmp
ARM: dts: append DTS file of pxa168
ARM: mmp: append OF support on pxa168
ARM: mmp: enable rtc clk in pxa168
i2c: pxa: add OF support
serial: pxa: add OF support
(plus update to v3.3-rc6)
Conflicts:
drivers/net/vmxnet3/vmxnet3_drv.c
Small vmxnet3 conflict with header size bug fix in 'net'.
Signed-off-by: David S. Miller <davem@davemloft.net>
The API model is changed from:
p = pinctrl_get(dev, "state1");
pinctrl_enable(p);
...
pinctrl_disable(p);
pinctrl_put(p);
p = pinctrl_get(dev, "state2");
pinctrl_enable(p);
...
pinctrl_disable(p);
pinctrl_put(p);
to this:
p = pinctrl_get(dev);
s1 = pinctrl_lookup_state(p, "state1");
s2 = pinctrl_lookup_state(p, "state2");
pinctrl_select_state(p, s1);
...
pinctrl_select_state(p, s2);
...
pinctrl_put(p);
This allows devices to directly transition between states without
disabling the pin controller programming and put()/get()ing the
configuration data each time. This model will also better suit pinconf
programming, which doesn't have a concept of "disable".
The special-case hogging feature of pin controllers is re-written to use
the regular APIs instead of special-case code. Hence, the pinmux-hogs
debugfs file is removed; see the top-level pinctrl-handles files for
equivalent data.
Signed-off-by: Stephen Warren <swarren@nvidia.com>
Acked-by: Dong Aisheng <dong.aisheng@linaro.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Since all that include/linux/if_ppp.h does is #include <linux/ppp-ioctl.h>,
this replaces the occurrences of #include <linux/if_ppp.h> with
#include <linux/ppp-ioctl.h>.
It also corrects an error in Documentation/networking/l2tp.txt, where
it referenced include/linux/if_ppp.h as the source of some definitions
that are actually now defined in include/linux/if_pppol2tp.h.
Signed-off-by: Paul Mackerras <paulus@samba.org>
Signed-off-by: David S. Miller <davem@davemloft.net>
pinctrl_register_mappings() already requires that every mapping table
entry have a non-NULL name field.
Logically, this makes sense too; drivers should always request a specific
named state so they know what they're getting. Relying on getting the
first mentioned state in the mapping table is error-prone, and a nasty
special case to implement, given that a given the mapping table may define
multiple states for a device.
Remove a small part of the documentation that talked about optionally
requesting a specific state; it's mandatory now.
Signed-off-by: Stephen Warren <swarren@nvidia.com>
Acked-by: Dong Aisheng <dong.aisheng@linaro.org>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
These two branches are a dependency for the at91 device tree changes,
so we pull them in here. at91/base2+cleanup will get merged through
the arm-soc cleanup2 branch, while the irqdomain tree will be sent
by Grant before this one gets integrated.
Conflicts:
drivers/rtc/rtc-at91sam9.c
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
* 'at91-3.4-base2+cleanup' of git://github.com/at91linux/linux-at91: (20 commits)
ARM: at91: properly sort dtb files in Makefile.boot
ARM: at91: add at91sam9g25ek.dts in Makefile.boot
ARM: at91/board-dt: drop default console
Atmel: move console default platform_device to serial driver
ARM: at91: merge SRAM Memory banks thanks to mirroring
ARM: at91: finally drop at91_sys_read/write
ARM: at91/rtc-at91sam9: pass the GPBR to use via resources
ARM: at91:rtc/rtc-at91sam9: ioremap register bank
ARM: at91/rtc-at91sam9: each SoC can select the RTT device to use
ARM: at91/PMC: make register base soc independent
ARM: at91/PMC: move assignment out of printf
ARM: at91/pm_slowclock: add runtime detection of memory contoller
ARM: at91: make sdram/ddr register base soc independent
ARM: at91: move at91rm9200 sdramc defines to at91rm9200_sdramc.h
ARM: at91/pm_slowclock: function slow_clock() accepts parameters
ARM: at91/pm_slowclock: rename register to named define
ARM: at91/ST: remove not needed casts
ARM: at91: make ST (System Timer) soc independent
ARM: at91: make matrix register base soc independent
ARM: at91/at91x40: remove use of at91_sys_read/write
Based on top of the at91/9x5, rmk/for-armsoc, at91/device-board,
at91/pm_cleanup and at91/base.
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
First step to debletcherising the vt console layer - pick a victim and fix
the locking
This is a nice simple object with its own rules so lets pick it out for
treatment. The user of the table already has a lock so we will also use the
same lock for updates.
Signed-off-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This reverts commit a50f724a43.
Sasha reported that this causes problems, so revert it.
Cc: Alan Cox <alan@linux.intel.com>
Cc: Jiri Slaby <jslaby@suse.cz>
Cc: Sasha Levin <levinsasha928@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This reverts commit d3bda5298a.
Sasha reported that this causes problems, so revert it.
Cc: Sasha Levin <levinsasha928@gmail.com>
Cc: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In DMA-operated uart, I found that rx data can be taken by the UART
interrupts during the DMA irq handler. pl011_int is occurred just
before it goes inside spin_lock_irq. When it returns to the callback,
DMA buffer already has been flushed. Then, pl011_dma_rx_chars gets
invalid data. So I add check for the residue as the patch bellow.
Signed-off-by: Chanho Min <chanho.min@lge.com>
Acked-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Without that fix machines having a s3c2442 CPU have something
like that in dmesg:
samsung-uart s3c2440-uart.0: could not find driver data
samsung-uart s3c2440-uart.1: could not find driver data
samsung-uart s3c2440-uart.2: could not find driver data
And serial is never initialized.
The previous log was obtained trough early printk on the gta02
machine.
Signed-off-by: Denis 'GNUtoo' Carikli <GNUtoo@no-log.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
drivers/tty/serial/mux.c included 'linux/tty.h' twice, remove
the duplicate.
Signed-off-by: Danny Kukawka <danny.kukawka@bisect.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This variable spread on every SoC that is using the atmel_serial.c
driver can be included directly into the latter.
This will allow to compile multiple soc in the same kernel.
Signed-off-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Cc: Hans-Christian Egtvedt <egtvedt@samfundet.no>
Cc: kernel@avr32linux.org
This patch allows the system to boot and enables the console and at least
some hardware drivers, as well as some platform error handling.
Tested on a variety of SGI Altix system without issues.
Signed-off-by: Dimitri Sivanich <sivanich@sgi.com>
Tested-by: Raymund Will <rw@suse.de>
Signed-off-by: Tony Luck <tony.luck@intel.com>
We changed the signature of the pin multiplexing functions to
handle any pin business, so fix up the Sirf driver to call this
new interface and rename some variables to make the semantics
understandable.
Cc: linux-serial@vger.kernel.org
Acked-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Acked-by: Barry Song <Baohua.Song@csr.com>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
* lpc32xx/drivers: (566 commits)
ARM: LPC32xx: ADC support for mach-lpc32xx
Includes an update to Linux 3.3-rc4
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
.device_fc is added in struct dma_slave_config recently. All user drivers, which
want DMA to be the flow controller must pass this field as false. As earlier
driver don't look to use this feature, mark it false for now.
Signed-off-by: Viresh Kumar <viresh.kumar@st.com>
Acked-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Vinod Koul <vinod.koul@linux.intel.com>
There are multiple users of this file from different source
paths now, and rather than have ../ paths in include statements,
just move the file to the linux header dir.
Suggested-by: David S. Miller <davem@davemloft.net>
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Acked-by: David S. Miller <davem@davemloft.net>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The receive FIFO wakeup latency estimate in the omap-serial driver is
three orders of magnitude too small. This effectively prevents the
MPU from going to a low-power state when CONFIG_CPU_IDLE=y. This is a
major power management regression and masks some other FIFO-related
bugs in the driver.
Fix by correcting the most egregious problem in the RX wakeup latency
estimate. There are several other flaws in the estimator; these will
be fixed by a separate patch series intended for 3.4.
The difference in low-power states with this patch can be observed via
debugfs in pm_debug/count.
This estimate does not have any effect when CONFIG_CPU_IDLE=n.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Cc: Alan Cox <alan@linux.intel.com>
Acked-by: Govindraj.R <govindraj.raja@ti.com>
Reviewed-by: Kevin Hilman <khilman@ti.com>
Tested-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Prevent OMAP UARTs from going idle while they are still transferring
data in PIO mode. This works around an oversight in the OMAP UART
hardware present in OMAP34xx and earlier: an idle UART won't send a
wakeup when the TX FIFO threshold is reached. This causes long delays
during data transmission when the MPU powerdomain enters a low-power
mode. The MPU interrupt controller is not able to respond to
interrupts when it's in a low-power state, so the TX buffer is not
refilled until another wakeup event occurs.
This fix changes the erratum i291 DMA idle workaround. Rather than
toggling between force-idle and no-idle, it will toggle between
smart-idle and no-idle. The important part of the workaround is the
no-idle part, so this shouldn't result in any change in behavior.
This fix should work on all OMAP UARTs. Future patches intended for
the 3.4 merge window will make this workaround conditional on a
"feature" flag, and will use the OMAP36xx+ TX event wakeup support.
Thanks to Kevin Hilman <khilman@ti.com> for mentioning the erratum i291
workaround, which led to the development of this approach.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Alan Cox <alan@linux.intel.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Acked-by: Govindraj.R <govindraj.raja@ti.com>
Reviewed-by: Kevin Hilman <khilman@ti.com>
Tested-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In the (default) PIO mode, use a one-byte RX FIFO threshold. The OMAP
UART IP blocks do not appear to be capable of waking the system under
an RX timeout condition. Since the previous RX FIFO threshold was 16
bytes, this meant that omap-serial.c did not become aware of any
received data until all those bytes arrived or until another UART
interrupt occurred. This made the serial console and presumably other
serial applications (GPS, serial Bluetooth) unusable or extremely
slow. A 1-byte RX FIFO threshold also allows the MPU to enter a
low-power consumption state while waiting for the FIFO to fill.
This can be verified using the serial console by comparing the
behavior when "0123456789abcde" is pasted in from another window, with
the behavior when "0123456789abcdef" is pasted in. Since the former
string is less than sixteen bytes long, the string is not echoed for
some time, while the latter string is echoed immediately.
DMA operation is unaffected by this patch.
Thanks to Russell King - ARM Linux <linux@arm.linux.org.uk> for some
additional information on the standard behavior of the RX timeout
event, which was used to improve this commit description.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Cc: Govindraj Raja <govindraj.r@ti.com>
Cc: Alan Cox <alan@linux.intel.com>
Cc: Russell King <linux@arm.linux.org.uk>
Reviewed-by: Kevin Hilman <khilman@ti.com>
Tested-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This allows altera_uart to be used for KGDB debugging over serial line.
Signed-off-by: Tobias Klauser <tklauser@distanz.ch>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The function has no users inside the tree and the nios2
(out-of-mainline) port doesn't use it either (anymore).
Signed-off-by: Tobias Klauser <tklauser@distanz.ch>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There's a real possibility of killing kernel threads that might
have issued use_mm(), so kthread's mm might become non-NULL.
This patch fixes the issue by checking for PF_KTHREAD (just as
get_task_mm()).
Suggested-by: Oleg Nesterov <oleg@redhat.com>
Signed-off-by: Anton Vorontsov <anton.vorontsov@linaro.org>
Acked-by: David Rientjes <rientjes@google.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
sysrq should grab the tasklist lock, otherwise calling force_sig() is
not safe, as it might race with exiting task, which ->sighand might be
set to NULL already.
Signed-off-by: Anton Vorontsov <anton.vorontsov@linaro.org>
Acked-by: David Rientjes <rientjes@google.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
pch_uart_hal_request() has parameters which it never uses, also
it is very short, so merge it with its caller to make code cleaner.
No functional changes at all.
Signed-off-by: Feng Tang <feng.tang@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The short get_msr() has some unnecessary code and only used once,
so merge it with its caller to make code cleaner. No functional
change at all.
Signed-off-by: Feng Tang <feng.tang@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This driver will be use as interfaces for multiple kinds of
devices like Bluetooth/GPS etc, this debug hook will make driver
debugging much easier.
Signed-off-by: Feng Tang <feng.tang@intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit 9bef3d4197
"serial: group all the 8250 related code together"
inadvertently swept up the m32r driver in the move, because
it had comments mentioning 8250 registers within it. However
these are only there by nature of the driver being based off
the 8250 source code -- the hardware itself does not actually
have any relation to the original 8250 style UARTs.
Reported-by: Jiri Slaby <jirislaby@gmail.com>
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
KDFONTOP(GET) currently fails with EIO when being run in a 32bit userland
with a 64bit kernel if the font width is not 8.
This is because of the setting of the KD_FONT_FLAG_OLD flag, which makes
con_font_get return EIO in such case.
This flag should *not* be set for KDFONTOP, since it's actually the whole
point of this flag (see comment in con_font_set for instance).
Signed-off-by: Samuel Thibault <samuel.thibault@ens-lyon.org>
Reviewed-by: Arnd Bergmann <arnd@arndb.de>
Cc: Greg Kroah-Hartman <gregkh@suse.de>
Cc: Arthur Taylor <art@ified.ca>
Cc: Jiri Slaby <jslaby@suse.cz>
Cc: Jiri Olsa <jolsa@redhat.com>
Cc: <stable@vger.kernel.org>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
On sparc, there is a build failure:
drivers/tty/serial/8250/8250.c:48:21: error: suncore.h: No such file or directory
drivers/tty/serial/8250/8250.c:3275: error: implicit declaration of function 'sunserial_register_minors'
drivers/tty/serial/8250/8250.c:3305: error: implicit declaration of function 'sunserial_unregister_minors'
this is due to commit 9bef3d4197
(serial: group all the 8250 related code together) moved these files
into 8250/ subdirectory, but forgot to change the reference
to drivers/tty/serial/suncore.h.
Cc: Paul Gortmaker <paul.gortmaker@windriver.com>
Signed-off-by: WANG Cong <xiyou.wangcong@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This should be added for EXYNOS4212 and EXYNOS4412 SoCs.
Cc: Thomas Abraham <thomas.abraham@linaro.org>
Cc: Greg Kroah-Hartman <gregkh@suse.de>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
KDFONTOP(GET) currently fails with EIO when being run in a 32bit userland
with a 64bit kernel if the font width is not 8.
This is because the compatibility layer introduced by e9216651 ("tty:
handle VT specific compat ioctls in vt driver") forces the addition of the
KD_FONT_FLAG_OLD flag, which makes con_font_get return EIO in such case.
This flag should *not* be set for KDFONTOP, since it's actually the whole
point of this flag (see comment in con_font_set for instance).
Signed-off-by: Samuel Thibault <samuel.thibault@ens-lyon.org>
Cc: Arnd Bergmann <arnd@arndb.de>
Cc: Arthur Taylor <art@ified.ca>
Cc: Jiri Slaby <jslaby@suse.cz>
Cc: Jiri Olsa <jolsa@redhat.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
devpts operations are protected by inode mutexes and dentry
refcounting. There is no need to hold BTM.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The code looks like:
if (tty->driver->subtype == PTY_TYPE_MASTER) {
...
if (tty->driver == ptm_driver)
But the second if is superfluous because only the ptm_driver is of
PTY_TYPE_MASTER subtype.
Also we can remove the #if now because devpts_pty_kill is defined as
an empty function for non-CONFIG_UNIX98_PTYS configs.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Use the helper in the rest of the tty drivers. This is a simple
replacement.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There are currently many cut&paste copies of what
tty_driver_install_tty does when custom ->install method is not
provided. Let's get rid of the copies and create a helper with this
setup code.
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Cc: Havard Skinnemoen <hskinnemoen@google.com>
Acked-by: Alan Cox <alan@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The receive FIFO wakeup latency estimate in the omap-serial driver is
three orders of magnitude too small. This effectively prevents the
MPU from going to a low-power state when CONFIG_CPU_IDLE=y. This is a
major power management regression and masks some other FIFO-related
bugs in the driver.
Fix by correcting the most egregious problem in the RX wakeup latency
estimate. There are several other flaws in the estimator; these will
be fixed by a separate patch series intended for 3.4.
The difference in low-power states with this patch can be observed via
debugfs in pm_debug/count.
This estimate does not have any effect when CONFIG_CPU_IDLE=n.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Cc: Alan Cox <alan@linux.intel.com>
Acked-by: Govindraj.R <govindraj.raja@ti.com>
Reviewed-by: Kevin Hilman <khilman@ti.com>
Tested-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Prevent OMAP UARTs from going idle while they are still transferring
data in PIO mode. This works around an oversight in the OMAP UART
hardware present in OMAP34xx and earlier: an idle UART won't send a
wakeup when the TX FIFO threshold is reached. This causes long delays
during data transmission when the MPU powerdomain enters a low-power
mode. The MPU interrupt controller is not able to respond to
interrupts when it's in a low-power state, so the TX buffer is not
refilled until another wakeup event occurs.
This fix changes the erratum i291 DMA idle workaround. Rather than
toggling between force-idle and no-idle, it will toggle between
smart-idle and no-idle. The important part of the workaround is the
no-idle part, so this shouldn't result in any change in behavior.
This fix should work on all OMAP UARTs. Future patches intended for
the 3.4 merge window will make this workaround conditional on a
"feature" flag, and will use the OMAP36xx+ TX event wakeup support.
Thanks to Kevin Hilman <khilman@ti.com> for mentioning the erratum i291
workaround, which led to the development of this approach.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Alan Cox <alan@linux.intel.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Acked-by: Govindraj.R <govindraj.raja@ti.com>
Reviewed-by: Kevin Hilman <khilman@ti.com>
Tested-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In the (default) PIO mode, use a one-byte RX FIFO threshold. The OMAP
UART IP blocks do not appear to be capable of waking the system under
an RX timeout condition. Since the previous RX FIFO threshold was 16
bytes, this meant that omap-serial.c did not become aware of any
received data until all those bytes arrived or until another UART
interrupt occurred. This made the serial console and presumably other
serial applications (GPS, serial Bluetooth) unusable or extremely
slow. A 1-byte RX FIFO threshold also allows the MPU to enter a
low-power consumption state while waiting for the FIFO to fill.
This can be verified using the serial console by comparing the
behavior when "0123456789abcde" is pasted in from another window, with
the behavior when "0123456789abcdef" is pasted in. Since the former
string is less than sixteen bytes long, the string is not echoed for
some time, while the latter string is echoed immediately.
DMA operation is unaffected by this patch.
Thanks to Russell King - ARM Linux <linux@arm.linux.org.uk> for some
additional information on the standard behavior of the RX timeout
event, which was used to improve this commit description.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Cc: Tomi Valkeinen <tomi.valkeinen@ti.com>
Cc: Govindraj Raja <govindraj.r@ti.com>
Cc: Alan Cox <alan@linux.intel.com>
Cc: Russell King <linux@arm.linux.org.uk>
Reviewed-by: Kevin Hilman <khilman@ti.com>
Tested-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>