Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Alexander reported that the new optimized handling of the RX fifo
causes random packet loss on Intel PCH C_CAN hardware.
After a few fruitless debugging sessions I got hold of a PCH (eg20t)
afflicted system. That machine does not have the CAN interface wired
up, but it was possible to reproduce the issue with the HW loopback
mode.
As Alexander observed correctly, clearing the NewDat flag along with
reading out the message buffer causes that issue on C_CAN, while D_CAN
handles that correctly.
Instead of restoring the original message buffer handling horror the
following workaround solves the issue:
transfer buffer to IF without clearing the NewDat
handle the message
clear NewDat bit
That's similar to the original code but conditional for C_CAN.
I really wonder why all user manuals (C_CAN, Intel PCH and some more)
recommend to clear the NewDat bit right away. The knows it all Oracle
operated by Gurgle does not unearth any useful information either. I
simply cannot believe that we are the first to uncover that HW issue.
Reported-and-tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
The RX buffer split causes packet loss in the hardware:
What happens is:
RX Packet 1 --> message buffer 1 (newdat bit is not cleared)
RX Packet 2 --> message buffer 2 (newdat bit is not cleared)
RX Packet 3 --> message buffer 3 (newdat bit is not cleared)
RX Packet 4 --> message buffer 4 (newdat bit is not cleared)
RX Packet 5 --> message buffer 5 (newdat bit is not cleared)
RX Packet 6 --> message buffer 6 (newdat bit is not cleared)
RX Packet 7 --> message buffer 7 (newdat bit is not cleared)
RX Packet 8 --> message buffer 8 (newdat bit is not cleared)
Clear newdat bit in message buffer 1
Clear newdat bit in message buffer 2
Clear newdat bit in message buffer 3
Clear newdat bit in message buffer 4
Clear newdat bit in message buffer 5
Clear newdat bit in message buffer 6
Clear newdat bit in message buffer 7
Clear newdat bit in message buffer 8
Now if during that clearing of newdat bits, a new message comes in,
the HW gets confused and drops it.
It does not matter how many of them you clear. I put a delay between
clear of buffer 1 and buffer 2 which was long enough that the message
should have been queued either in buffer 1 or buffer 9. But it did not
show up anywhere. The next message ended up in buffer 1. So the
hardware lost a packet of course without telling it via one of the
error handlers.
That does not happen on all clear newdat bit events. I see one of 10k
packets dropped in the scenario which allows us to reproduce. But the
trace looks always the same.
Not splitting the RX Buffer avoids the packet loss but can cause
reordering. It's hard to trigger, but it CAN happen.
With that mode we use the HW as it was probably designed for. We read
from the buffer 1 upwards and clear the buffer as we get the
message. That's how all microcontrollers use it. So I assume that the
way we handle the buffers was never really tested. According to the
public documentation it should just work :)
Let the user decide which evil is the lesser one.
[ Oliver Hartkopp: Provided a sane config option and help text and
made me switch to favour potential and unlikely reordering over
packet loss ]
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
The driver handles pointlessly TWO interrupts per packet. The reason
is that it enables the status interrupt which fires for each rx and tx
packet and it enables the per message object interrupts as well.
The status interrupt merily acks or in case of D_CAN ignores the TX/RX
state and then the message object interrupt fires.
The message objects interrupts are only useful if all message objects
have hardware filters activated.
But we don't have that and its not simple to implement in that driver
without rewriting it completely.
So we can ditch the message object interrupts and handle the RX/TX
right away from the status interrupt. Instead of TWO we handle ONE.
Note: We must keep the TXIE/RXIE bits in the message buffers because
the status interrupt alone is not reliable enough in corner cases.
If we ever have the need for HW filtering, then this code needs a
complete overhaul and we can think about it then. For now we prefer a
lower interrupt load.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
On D_CAN the RXOK, TXOK and LEC bits are cleared/set on read of the
status register. No need to update them.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Instead of writing to the message object we can simply clear the
NewDat bit with the get method.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
If the allocation of the error skb fails, we still want to see the
error statistics.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Reading the LEC type with
return (mode & ENABLED) && (status & LEC_MASK);
is not guaranteed to return (status & LEC_MASK) if the enabled bit in
mode is set. It's guaranteed to return 0 or !=0.
Remove the inline function and call unconditionally into the
berr_handling code and return early when the reporting is disabled.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
If the allocation of an error skb fails, the state change handling
returns w/o doing any work. That leaves the interface in a wreckaged
state as the internal status is wrong.
Split the interface handling and the skb handling.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
There is no guarantee that the skb is in the same state after calling
net_receive_skb(). It might be freed or reused. Not really harmful as
its a read access, except you turn on the proper debugging options
which catch a use after free.
The whole can subsystem is full of this. Copy and paste ....
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
The state change handler is called with device interrupts disabled
already. So no point in disabling them again when we enter bus off
state.
But what's worse is that we reenable the interrupts at the end of NAPI
poll unconditionally. So c_can_start() which is called from the
restart timer can trigger interrupts which confuse the hell out of the
half reinitialized driver/hw.
Remove the pointless device interrupt disable in the BUS_OFF handler
and prevent reenabling the device interrupts at the end of the poll
routine when the current state is BUS_OFF.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
c_can_start() enables interrupts way too early. The first enabling
happens when setting the control mode in c_can_chip_config() and then
again at the end of the function.
But that happens before napi_enable() and that means that an interrupt
which comes in will disable interrupts again and call napi_schedule,
which ignores the request and the later napi_enable() is not making
thinks work either. So the interface is up with all device interrupts
disabled.
Move the device interrupt after napi_enable() and add it to the other
callsites of c_can_start() in c_can_set_mode() and c_can_power_up()
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
All type checks in c_can.c are != BOSCH_D_CAN so nobody noticed so far
that the pci code does not update the type information.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Alexander Stein <alexander.stein@systec-electronic.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
This fixes a seg fault on 'ethtool -A' entry if the
interface is down. Obviously we need to have the
phy device initialized / "connected" (see of_phy_connect())
to be able to advertise pause frame capabilities.
Fixes: 23402bddf9
Signed-off-by: Claudiu Manoil <claudiu.manoil@freescale.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
o In case QLC_83XX_MBX_CMD_NO_WAIT command type the calling
function does not free the memory as it does not wait for
response. So free it when get a response from adapter after
sending the command.
Signed-off-by: Rajesh Borundia <rajesh.borundia@qlogic.com>
Signed-off-by: Shahed Shaikh <shahed.shaikh@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Some firmware versions fails to reset the lock during
initialization. Force reset firmware API lock during driver
probe to ensure lock availability.
Signed-off-by: Sony Chacko <sony.chacko@qlogic.com>
Signed-off-by: Shahed Shaikh <shahed.shaikh@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
There are two breaks missing there. The result is that userspace
receives multiple messages which might be confusing.
Introduced-by: 3d249d4c "net: introduce ethernet teaming device"
Signed-off-by: Jiri Pirko <jiri@resnulli.us>
Signed-off-by: David S. Miller <davem@davemloft.net>
I was told that the Cadence macb driver is also useful on Microblaze.
Signed-off-by: Jean Delvare <jdelvare@suse.de>
Cc: Nicolas Ferre <nicolas.ferre@atmel.com>
Cc: David S. Miller <davem@davemloft.net>
Cc: Michal Simek <monstr@monstr.eu>
Cc: Mark Brown <broonie@kernel.org>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Redefine some macros that were conditioned upon SMC_DEBUG level.
By allowing compiler to verify parameters used by these macros
unconditionally, we can flag compilation failures.
Compiler will still optimize out the unused code path depending on
SMC_DEBUG, so this is a net gain.
Signed-off-by: Joe Perches <joe@perches.com>
Signed-off-by: Zi Shen Lim <zlim.lnx@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The goal of this patch is to fix rtnelink notification. The main problem was
about notification for fdb entry with more than one remote. Before the patch,
when a remote was added to an existing fdb entry, the kernel advertised the
first remote instead of the added one. Also when a remote was removed from a fdb
entry with several remotes, the deleted remote was not advertised.
Signed-off-by: Nicolas Dichtel <nicolas.dichtel@6wind.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
In ksz9021_load_values_from_of() val2 to val4 aren't tested against their
initialization value.
This causes the test to always succeed, and this value to be used as if it
was loaded from the devicetree instead of being ignored, in case of a
missing/invalid property in the ethernet OF device node.
As a result, the value "0" is written to the relevant registers.
Change the conditions to test against the right initialization value.
Signed-off-by: Hubert Chaumette <hchaumette@adeneo-embedded.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
When SMC_DEBUG >= 2, we hit the following compilation error:
drivers/net/ethernet/smsc/smc91x.c:85:0:
drivers/net/ethernet/smsc/smc91x.c: In function ‘smc_findirq’:
drivers/net/ethernet/smsc/smc91x.c:1784:9: error: ‘dev’ undeclared (first use in this function)
DBG(2, dev, "%s: %s\n", CARDNAME, __func__);
^
Fix it by passing in the appropriate netdev pointer.
Signed-off-by: Zi Shen Lim <zlim.lnx@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch adds phy_found error path when there is no phy device
and changes bus_name.
Signed-off-by: Byungho An <bh74.an@samsung.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This patch moves cksum_ctl to tx_rd_des23 from cksum_pktlen for correct checksum
offloading and modifies size for Tx/Rx descriptor.
Signed-off-by: Byungho An <bh74.an@samsung.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Execute "ethtool -L eth0 combined 0" in guest, if multiqueue
is enabled, virtnet_send_command() will return -EINVAL error,
there is a validation in QEMU.
But if multiqueue is disabled, virtnet_set_queues() will just
return zero (success). We should return error for this situation.
Signed-off-by: Amos Kong <akong@redhat.com>
Acked-by: Jason Wang <jasowang@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The MAC address retrieved from dt was not actually written to the
hardware. This meant proper communication was only possible after
changing the MAC address.
Fix that by always writing the mac address during probing.
Signed-off-by: Max Schwarz <max.schwarz@online.de>
Acked-by: Heiko Stuebner <heiko@sntech.de>
Tested-by: Heiko Stuebner <heiko@sntech.de>
Signed-off-by: David S. Miller <davem@davemloft.net>
Add \n at the end of messages where missing, remove all \r.
Reported-by: Joe Perches <joe@perches.com>
Signed-off-by: Jakub Kicinski <kubakici@wp.pl>
Tested-by: Aaron Brown <aaron.f.brown@intel.com>
Tested-by: Phil Schmitt <phillip.j.schmitt@intel.com>
Tested-by: Kavindya Deegala <kavindya.s.deegala@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
Time stamping resources are per-interface so there is no need
to keep separate last_rx_timestamp for each Rx ring, move
last_rx_timestamp to the adapter structure.
With last_rx_timestamp inside adapter, ixgbe_ptp_rx_hwtstamp()
inline function is reduced to a single if statement so it is
no longer necessary. If statement is placed directly in
ixgbe_process_skb_fields() fixing likely/unlikely marking.
Checks for q_vector or adapter to be NULL are superfluous.
Comment about taking I/O hit is a leftover from previous design.
Signed-off-by: Jakub Kicinski <kubakici@wp.pl>
Tested-by: Phil Schmitt <phillip.j.schmitt@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
RQDPC on i210/i211 is R/W not ReadClear. Clear after reading.
Signed-off-by: Todd Fujinaka <todd.fujinaka@intel.com>
Tested-by: Aaron Brown <aaron.f.brown@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
Fix following compilation warning:
drivers/net/ethernet/intel/e1000e/netdev.c:6238:12: warning
‘e1000e_pm_thaw’ defined but not used [-Wunused-function]
static int e1000e_pm_thaw(struct device *dev)
^
Signed-off-by: Hiroaki SHIMODA <shimoda.hiroaki@gmail.com>
Tested-by: Aaron Brown <aaron.f.brown@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
When changing the interface mtu, the driver starts with a value
that doesn't include VLAN_HLEN. Later tests in the driver
set the rx_buffer_len based on the mtu. As a result, when
the user increases the mtu to 1504 (to support 802.1AD for example),
the driver rx_buffer_len does not change and frames longer
the 1522 bytes are rejected as too long.
Include VLAN_HLEN from the start so that an user mtu greater then
1500 bytes is correctly reflected in the driver rx_buffer_len.
CC: e1000-devel@lists.sourceforge.net
Signed-off-by: Vlad Yasevich <vyasevic@redhat.com>
Tested-by: Aaron Brown <aaron.f.brown@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
As reported by Eric Dumazet, the i40e driver was allowing the hardware
to replicate the PSH flag on all segments of a TSO operation.
This patch fixes the first/middle/last TCP flags settings which
makes the TSO operations work correctly.
With this change we are now configuring the CWR bit to only be set
in the first packet of a TSO, so this patch also enables TSO_ECN,
in order to advertise to the stack that we do the right thing
on the wire.
Reported-by: Eric Dumazet <eric.dumazet@gmail.com>
Signed-off-by: Jesse Brandeburg <jesse.brandeburg@intel.com>
Tested-by: Kavindya Deegala <kavindya.s.deegala@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
John W. Linville says:
====================
pull request: wireless 2014-04-17
Please pull this batch of fixes intended for the 3.15 stream...
For the mac80211 bits, Johannes says:
"We have a fix from Chun-Yeow to not look at management frame bitrates
that are typically really low, two fixes from Felix for AP_VLAN
interfaces, a fix from Ido to disable SMPS settings when a monitor
interface is enabled, a radar detection fix from Michał and a fix from
myself for a very old remain-on-channel bug."
For the iwlwifi bits, Emmanuel says:
"I have new device IDs and a new firmware API. These are the trivial
ones. The less trivial ones are Johannes's fix that delays the
enablement of an interrupt coalescing hardware until after association
- this fixes a few connection problems seen in the field. Eyal has a
bunch of rate control fixes. I decided to add these for 3.15 because
they fix some disconnection and packet loss scenarios which were
reported by the field. I also have a fix for a memory leak that
happens only with a very new NIC."
Along with those...
Amitkumar Karwar fixes a couple of problems relating to driver/firmware
interactions in mwifiex.
Christian Engelmayer avoids a couple of potential memory leaks in
the new rsi driver.
Eliad Peller provides a wl18xx mailbox alignment fix for problems
when using new firmware.
Frederic Danis adds a couple of missing debugging strings to the
cw1200 driver.
Geert Uytterhoeven adds a variable initialization inside of the
rsi driver.
Luciano Coelho patches the wlcore code to ignore dummy packet events
in PLT mode in order to work around a firmware bug.
====================
Signed-off-by: David S. Miller <davem@davemloft.net>
The patch fixes a problem with dropped jumbo frames after usage of
'ethtool -G ... rx'.
Scenario:
1. ip link set eth0 up
2. ethtool -G eth0 rx N # <- This zeroes rx-jumbo
3. ip link set mtu 9000 dev eth0
The ethtool command set rx_jumbo_pending to zero so any received jumbo
packets are dropped and you need to use 'ethtool -G eth0 rx-jumbo N'
to workaround the issue.
The patch changes the logic so rx_jumbo_pending value is changed only if
jumbo frames are enabled (MTU > 1500).
Signed-off-by: Ivan Vecera <ivecera@redhat.com>
Acked-by: Michael Chan <mchan@broadcom.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
This is for a system with fixed assignments of input and output pins
(various variants of Kontron COMe).
Signed-off-by: Guenter Roeck <linux@roeck-us.net>
Signed-off-by: David S. Miller <davem@davemloft.net>
Some systems using mdio-gpio may use active-low gpio pins
(eg with inverters or FETs connected to all or some of the
gpio pins).
Signed-off-by: Guenter Roeck <linux@roeck-us.net>
Signed-off-by: David S. Miller <davem@davemloft.net>
This simplifies error path and deinit/removal functions.
Signed-off-by: Guenter Roeck <linux@roeck-us.net>
Tested-by: Chris Healy <cphealy@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The mlx4 driver is triggering schedules while atomic inside
mlx4_en_netpoll:
spin_lock_irqsave(&cq->lock, flags);
napi_synchronize(&cq->napi);
^^^^^ msleep here
mlx4_en_process_rx_cq(dev, cq, 0);
spin_unlock_irqrestore(&cq->lock, flags);
This was part of a patch by Alexander Guller from Mellanox in 2011,
but it still isn't upstream.
Signed-off-by: Chris Mason <clm@fb.com>
cc: stable@vger.kernel.org
Acked-By: Amir Vadai <amirv@mellanox.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Commit 5445eaf309 ('mvneta: Try to fix mvneta when compiled as
module') fixed the mvneta driver to make it work properly when loaded
as a module in SGMII configuration, which was tested successful by the
author on the Armada XP OpenBlocks AX3, which uses SGMII.
However, some other platforms, namely the Armada XP GP don't use
SGMII, but a QSGMII connection between the MAC and the PHY, and this
case was not supported by the mvneta driver, which was relying on
configuration put in place by the bootloader. While this works when
the mvneta driver is built-in (because clocks are not gated), it
breaks when mvneta is built as a module, because the clock is gated
(all configuration is lost) and then re-enabled when the mvneta driver
is loaded.
In order to support all of RGMII, SGMII and QSGMII, this commit
reworks how the PHY interface configuration is done, and simplifies
it: it removes the mvneta_port_sgmii_config() and
mvneta_gmac_rgmii_set() functions, which were strange because
mvneta_gmac_rgmii_set() was called in all cases, even for SGMII
configurations. Also, the mvneta_gmac_rgmii_set() function was taking
a boolean as argument, which was always true.
Instead, all the PHY interface configuration logic is moved into the
mvneta_port_power_up() function, in a much simpler 'switch' construct,
with four cases:
- QSGMII: the RGMIIEn bit, the PCSEn bit in GMAC_CTRL_2 are set, and
the SERDES is configured in QSGMII. Technically speaking,
configuring the SERDES of the first port would be sufficient, but
it is simpler to do it on all ports.
- SGMII: the RGMIIEn bit, the PCSEn bit in GMAC_CTRL_2 are set, and
the SERDES is configured as SGMII.
- RGMII: the RGMIIEn bit in GMAC_CTRL_2 is set. The PCSEn bit is kept
cleared, and no SERDES configuration is done, because RGMII is not
using SERDES lanes.
- other: an error is returned. For this reason, the
mvneta_port_power_up() now returns an int instead of nothing, and
the return value is checked by mvneta_probe().
This has been successfully tested on:
* Armada XP DB, which has two RGMII and two SGMII connections
* Armada XP GP, which uses QSGMII for its four interfaces
* Armada 370 Mirabox, which has two RGMII connections
Signed-off-by: Thomas Petazzoni <thomas.petazzoni@free-electrons.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
When an MCDI command times out (whether or not we find it
completed when we poll), call efx_mcdi_abandon(), which tells
all subsequent MCDI calls to fail-fast, and queues up an FLR.
Because an FLR doesn't lead to receiving any reboot even from
the MC (unlike most other types of reset), we have to call
efx_ef10_reset_mc_allocations.
In efx_start_all(), if a reset (of any kind) is pending, we
bail out.
Without this, attempts to reconfigure (e.g. change mtu) can
cause driver/mc state inconsistency if the first MCDI call
triggers an FLR.
For similar reasons, on EF10, in
efx_reset_down(method=RESET_TYPE_MCDI_TIMEOUT), set the number
of active queues to zero before calling efx_stop_all().
And, on farch, in efx_reset_up(method=RESET_TYPE_MCDI_TIMEOUT),
set active_queues and flushes pending & outstanding to zero.
efx_mcdi_mode_{poll,event}() should not take us out of fail-fast
mode. Instead, this is done by efx_mcdi_reset() after the FLR
completes.
The new FLR reset_type RESET_TYPE_MCDI_TIMEOUT doesn't really
fit into the hierarchy of reset 'scopes' whereby efx_reset()
decides some resets subsume others. Thus, it uses separate logic.
Also, fixed up some inconsistency around RESET_TYPE_MC_BIST,
which was in the wrong place in that hierarchy.
Signed-off-by: Shradha Shah <sshah@solarflare.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The wrong max fw size was being used and causing false
"too big" errors running ethtool -f.
Signed-off-by: Steve Wise <swise@opengridcomputing.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Function qlcnic_setup_tss_rss_intr() might enter endless
loop in case pci_enable_msix() contiguously returns a
positive number of MSI-Xs that could have been allocated.
Besides, the function contains 'err = -EIO;' assignment
that never could be reached. This update fixes the
aforementioned issues.
Cc: Shahed Shaikh <shahed.shaikh@qlogic.com>
Cc: Dept-HSGLinuxNICDev@qlogic.com
Cc: netdev@vger.kernel.org
Cc: linux-pci@vger.kernel.org
Signed-off-by: Alexander Gordeev <agordeev@redhat.com>
Acked-by: Shahed Shaikh <shahed.shaikh@qlogic.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
In the dst->output() path for ipv4, the code assumes the skb it has to
transmit is attached to an inet socket, specifically via
ip_mc_output() : The sk_mc_loop() test triggers a WARN_ON() when the
provider of the packet is an AF_PACKET socket.
The dst->output() method gets an additional 'struct sock *sk'
parameter. This needs a cascade of changes so that this parameter can
be propagated from vxlan to final consumer.
Fixes: 8f646c922d ("vxlan: keep original skb ownership")
Reported-by: lucien xin <lucien.xin@gmail.com>
Signed-off-by: Eric Dumazet <edumazet@google.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Sometimes when command timeout occurs due to a firmware or
hardware bug, there may be some synchronous commands in command
queue. These commands are never downloaded to firmware causing
hung task warnings. This patch replaces wait_event_interruptible
call with wait_event_interruptible_timeout to fix the issue.
Signed-off-by: Amitkumar Karwar <akarwar@marvell.com>
Signed-off-by: Avinash Patil <patila@marvell.com>
Signed-off-by: Bing Zhao <bzhao@marvell.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
During extended scan, SCAN report event is always followed by
command response. Sometimes It is observed that command response
is processed before SCAN report which leads to a crash, because
current command node is cleared while handling the response.
This patch makes sure that driver's main thread gives priority
to events over command responses.
Signed-off-by: Amitkumar Karwar <akarwar@marvell.com>
Signed-off-by: Maithili Hinge <maithili@marvell.com>
Signed-off-by: Bing Zhao <bzhao@marvell.com>
Signed-off-by: John W. Linville <linville@tuxdriver.com>
In cosa driver, udelay with more than 20000 may cause __bad_udelay.
Use msleep for instead.
Signed-off-by: Li, Zhen-Hua <zhen-hual@hp.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
The __at86rf230_read_subreg function don't mask and shift register
contents which it should do. This patch adds the necessary masks and
shift operations in this function.
Since we have csma support this can make some trouble on state changes.
Since CSMA support turned on some bits in the TRX_STATUS register that
used to be zero, not masking broke checking of the TRX_STATUS field
after commanding a state change.
Signed-off-by: Alexander Aring <alex.aring@gmail.com>
Reviewed-by: Werner Almesberger <werner@almesberger.net>
Signed-off-by: David S. Miller <davem@davemloft.net>