arm64: dts: m3ulcb: Fix EthernetAVB PHY timing

Set PHY rxc-skew-ps to 1500 and all other values to their default values.

This is intended to to address failures in the case of 1Gbps communication
using the salvator-x board with the KSZ9031RNX phy. This has been
reported to occur with both the r8a7795 (H3) and r8a7796 (M3-W) SoCs.

Based in a similar patch for the r8a7796 salvator-x by Kazuya Mizuguchi.

Signed-off-by: Simon Horman <horms+renesas@verge.net.au>
This commit is contained in:
Simon Horman 2017-04-18 10:03:18 +09:00
parent d2ae6fedc4
commit bdb3656e4c

View File

@ -169,18 +169,7 @@ &avb {
status = "okay";
phy0: ethernet-phy@0 {
rxc-skew-ps = <900>;
rxdv-skew-ps = <0>;
rxd0-skew-ps = <0>;
rxd1-skew-ps = <0>;
rxd2-skew-ps = <0>;
rxd3-skew-ps = <0>;
txc-skew-ps = <900>;
txen-skew-ps = <0>;
txd0-skew-ps = <0>;
txd1-skew-ps = <0>;
txd2-skew-ps = <0>;
txd3-skew-ps = <0>;
rxc-skew-ps = <1500>;
reg = <0>;
interrupt-parent = <&gpio2>;
interrupts = <11 IRQ_TYPE_LEVEL_LOW>;